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A source on oil and gas well drilling ©If anything published on this channel infringe any patent, copyright, or other intellectual property rights claimed by third parties, please let us know and we will remove it. @Drilling_zone

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Kanal postlari
⚠️⚓ Jack-Up Platform Capsize During Rig Move Operation In offshore operations, risk is always present but few events are as sudden and severe as the capsize of a jack-up platform. This footage captures the exact moment stability was lost during a rig move, turning a routine operation into a critical incident within seconds. Such incidents highlight the importance of professional training, operational discipline, and strict adherence to safety procedures across the offshore industry. Key Lessons for Offshore Professionals 🔹 Comprehensive planning and risk assessment are mandatory for every rig move 🔹 Soil investigation and leg penetration analysis must be accurate and fully validated 🔹 Weather windows must be strictly respected small changes can have major consequences 🔹 Clear coordination between towing vessels, rig crew, and marine control is essential 🔹 Emergency preparedness and drills are vital they save lives Incidents like this reinforce why procedures, standards, and continuous training must never be compromised. Behind every offshore structure are people relying on safe decision-making and disciplined execution. Carditis

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Field Experience: Diagnosing a BHA Washout During a drilling operation, a gradual reduction in SPP was observed, eventually reaching 500 psi. After monitoring the trend and evaluating possible causes, the decision was made to POOH and inspect the drill string and BHA for signs of a washout. Upon inspection, a significant washout was found at the connection between the string stabilizer pin (upper component) and the float sub box (lower component), as shown in the attached photos. Based on the washout geometry visible on both components, which failure mechanism do you believe occurred first? Scenario 1: The float sub box developed a crack or defect first, initiating the washout and subsequently damaging the stabilizer pin connection. Scenario 2: The stabilizer pin developed a crack or defect first, initiating the washout and subsequently damaging the float sub box connection. I am interested to hear the opinions of drilling, L/MWD, directional drilling, and drilling tool specialists. Which scenario would you support, and what evidence from the washout pattern leads you to that conclusion? ✍ Credit
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